Right well I've done a compression test and all are 140-145 cold and 130-135 hot.
An inspection inside the chambers 2nd 3rd and 4th (cold) they "looked" oil filled, however after the "blast out" the the pistons have cleaned up and the smoke has reduced some what, but it is still noticeable. (plugs look good too)
I also cleaned up the intercooler pipes and ancillaries before I went out for a drive. After my return from the "blast out" they have a small amount of oil (film) around the pipe, but that could be down to what has been left over from when I was out previous/the oil residue that's been left in there.
At the moment, I still think it was the turbo seals and perhaps they've sorted out the problem when they took it apart?
However I've still got the boost problems. The symptoms are still the same: when introducing the power slowly the boost sometimes hits 0.8 bar, mainly 1.1bar and when I change gear at speed and immediately apply the power (foot the floor) the boost gauge shoots (peaks) still around 1.3 / 1.4 bar and then falls back to 1.1 bar???
Looking at the actuator, it seems like its not moved at all before it went away? How do you "check" of the actuator is working correctly?