just a quicky post , have been running my R since rebuild for a few months now .. with the help from martyn at alan jeffery engineering in plymouth , the car has been running at a low boost setting of around 310 bhp @1.bar and a high boost of 411bhp @1.4 bar . a lovely smooth map and the car has never ran so nice .. anyhows , i had the car in all last week for rear discs n pads and asked martyn to remap with a tad more boost .. the car now has 3 settings 310 /380/ and a new high setting of 456 bhp at 1.6 bar .... quick just doesnt justify the performance ... so set off on aroad trip this weekend from cornwall to stafford en route to alton towers .. car ran lovely all the way up and in and around alton ... set off yesterday to head to bristol shopping and then on home to cornwall ... had been running around on mid setting , as i join m6 flicked to high boost and attacked the on ramp .. absoloutly rapid !!!.. a few miles down the road whilst toeing it in fifth, hit like a fuel cut and car almost cuts out ... shit ... pull onto hard shoulder and instantly assume its the lead that comes out the bottom of my coil ... (one of the plug clips has snapped and i have a cable tie holding plug in , this has popped off before and gives a similar effect) to my dismay no... coil lead is still in !!... so call the AA and wait .. flat bed arrives and takes us to nearest services .. here another AA mechanic looks briefly and whips out a plug , the car is missing like its on 3 , black smoke out the back .. he checks all plugs are firing and engine doesnt change when plug leads are one by one removed ... his verdict .. either blown valve or piston (.. so we get flat bedded all the way home at 56 mph .. me in a foul mood declaring war on the R .. thats it im gonna start breaking it tommorrow .. not wasting another penny on this unreliable shitbox.. then i thought id call our very own guru pulsarbob.. i left a message and several hrs later just as we were dropping the car outside alan jefferys bob gets back to me ... i give bob the symptoms and bob tells me exactly what the problem is , and hey presto just like he said i spot the left hand front mount boost /intercooler pipe hanging off .. i wait for AA man to leave , re attach the pipe and car is back to normal ... massive grin appears back on my face .... and i saved £60 .00 in fuel ..... i am very un mechanically minded, and im sure its something a lot of owners may have sussed themselves , but a MASSIVE thanks goes out to bobby for being available to take a call and call me back on a sunday .. the man is an invaluable asset to this club .. thankyou bob... anyway , i will be putting an updated post in members Rs soon , but for now i ll attach the dyno printout
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