Now then everyone,
Please can I have some opinions on the below circs! Very long, but left me stumped!
Over past few months I have fitted to my car
Turbo Technics stage one hybrid (was with Hiteq when I bought it and given the OK, no play in shaft etc when I checked it)
550 Sards
And replaced my stolen SAFC 2
Engine internals are standard with filter, plugs, exhaust, walbro etc on. (Basic mods) plus an ARC TMIC
Went to John Nobles yesterday to have it on the dyno. Had some trouble on the way there but was the air con pumps giving up, but the good lads there simply put on a smaller belt missing out the A/C. The car did however boil its coolant whilst sat waiting because the fans didn’t come in, one off, were fine the rest of the day, also the ABS light came on the dash when pump started its noises, again was fine when I got my car back. Just some background if it means anything...
Car got on the dyno and after 2 hours + it put out .......254.9bhp @ 1.2 bar! :sad: Daz the operator said he wasn’t sure what it was, the 550's were having to get knocked down on the AFC so fuel was there, and boost was held solidly. No fault codes. Only thing he said he could think of was det sensor was playing up and was retarding the ignition, BUT on SAFC readings (I know not exact) were good and as they should be, peaked at 38 on a good 40 minute blast back from Doncaster to my house
BUT this is the thing, the car is very fast compared to what it was! On the powergraph it just dies at 4000 RPM (will post it up) but it does not act like that, power full on til the redline, I’m well pleased with it to be honest! And it was running 1.3 bar/313bhp before....donpulsar on here can vouch for this as he was in the car! (Thanks again Steve ) (PS: Steves car has full 3" inc elbow turbo back exhaust, basically same mods as mine, on multichecker, I know again not exact, is running 280ISH, and was keeping chase on the way there running .7 bar (dusting off a Megane 225 :lol: ), so its not been too slouchy recently)
What’s going on!
THIS IS NOT A DISS ON JOHN NOBLES, THEY WERE ACE THE WHOLE DAY SORTED ME OUT WHEN IT WAS BEING A LITTLE S**T :lol:
Just want some idea why it hooned around on the road straight after it put out that pathetic figure on dyno!!!
Dan
Please can I have some opinions on the below circs! Very long, but left me stumped!
Over past few months I have fitted to my car
Turbo Technics stage one hybrid (was with Hiteq when I bought it and given the OK, no play in shaft etc when I checked it)
550 Sards
And replaced my stolen SAFC 2
Engine internals are standard with filter, plugs, exhaust, walbro etc on. (Basic mods) plus an ARC TMIC
Went to John Nobles yesterday to have it on the dyno. Had some trouble on the way there but was the air con pumps giving up, but the good lads there simply put on a smaller belt missing out the A/C. The car did however boil its coolant whilst sat waiting because the fans didn’t come in, one off, were fine the rest of the day, also the ABS light came on the dash when pump started its noises, again was fine when I got my car back. Just some background if it means anything...
Car got on the dyno and after 2 hours + it put out .......254.9bhp @ 1.2 bar! :sad: Daz the operator said he wasn’t sure what it was, the 550's were having to get knocked down on the AFC so fuel was there, and boost was held solidly. No fault codes. Only thing he said he could think of was det sensor was playing up and was retarding the ignition, BUT on SAFC readings (I know not exact) were good and as they should be, peaked at 38 on a good 40 minute blast back from Doncaster to my house
BUT this is the thing, the car is very fast compared to what it was! On the powergraph it just dies at 4000 RPM (will post it up) but it does not act like that, power full on til the redline, I’m well pleased with it to be honest! And it was running 1.3 bar/313bhp before....donpulsar on here can vouch for this as he was in the car! (Thanks again Steve ) (PS: Steves car has full 3" inc elbow turbo back exhaust, basically same mods as mine, on multichecker, I know again not exact, is running 280ISH, and was keeping chase on the way there running .7 bar (dusting off a Megane 225 :lol: ), so its not been too slouchy recently)
What’s going on!
THIS IS NOT A DISS ON JOHN NOBLES, THEY WERE ACE THE WHOLE DAY SORTED ME OUT WHEN IT WAS BEING A LITTLE S**T :lol:
Just want some idea why it hooned around on the road straight after it put out that pathetic figure on dyno!!!
Dan